John S's Journal
Home Page: John S
Eugene, OR, USA
| Total Posts: 182 | Latest Post: 2026-03-25 |
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Engine and gearbox are out and clean as a whistle. Engine is in primer as are lots of the bolt on ancillaries. Parts have arrived. New B&B 3 piece clutch kit, new mounts, lots of gaskets, brake & clutch MC's, slave cylinder and hose,etc. Pedal box stripped, painted and MC's installed.
Flywheel is surfaced and ready to go.
Next is to get all of the engine and components painted, reinstall all the freshly painted bits, install new seals, install the clutch components and mate the engine and gearbox back up. When that is done, I'll move on to the engine bay cleanup and respray.
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oil and filter. With the car still up on jacks it was time to see if the car was going to run. The engine ran when I had it towed home almost 3 years ago so with the distributor unchanged and the engine wasn't touched, in theory it should fire. And it did but carburettors need some fine tuning.Time to check the clutch work that I did which was how I purchased the car. The owner needed his garage space and the clutch was gone so with the engine running I was able to run it through a couple of gears while it was still up in the air. All good so one step closer.
Last week it was time to put together some headlight and horns relays since the grill and bumper are still off. I had some aluminum c-channel laying around that was a perfect fit over the radiator support on the passenger side. Gathered up some correct color wire from an old harness, bought some cube relays and worked my way through the process of checking all lights with the help of a battery charger and some jumpers. Got all of them working except the high beams and flash to pass. One horn was dead. Opened up the column to get at the switches and discovered a mess. Wiper switch is beyond saving and the directional switch was better but couldn't get the high beams and the horn push was non-existent so it might be from the wrong model year. New switches ordered. High tone horn dissected and after much cleaning and a new gasket made, reassembled and got it working. Painted and installed.
This weekend it was time to check the valves and the timing. Adjusted the valves and timing and tweaked the HS4's a little and smoothed out the idle quite a bit. Still not great but good enough to take it for my first ever drive in this car. Off the stands, aired up the tires and cautiously checked the brakes and first and reverse gear. Decided to get it out in the sun and since we have a steep driveway, positioned it so that I could drive it forwards down the driveway. Quiet streets because of the shelter at home order so without a hood, expired plates and no turn signal switches it was time to see how it would do. Finally! I have a running, driving and stopping car. But it's not done. Stay tuned.
Another look. Corner was broken where the mounting bolt passes through. Bent bolt acting as a mounting stud.
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Running much better now so decided to focus on putting the console back in and wiring switches and lights up. Hazards weren’t working when I bought the car and had it towed home. At the time, I put a battery in and confirmed it was going to be a worthwhile project so it went right into the garage for a clutchectomy and lots of might as well jobs. Got the hazard switch wired up but fused brown wire to the switch was dead. Further investigation and the wire is toast up into the loom behind the dash. The PO had a cobbled up stereo installation in the console. Now I know why the radio didn’t work and the hazards as well. So it’s dash removal time.
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Running much better now so decided to focus on putting the console back in and wiring switches and lights up. Hazards weren’t working when I bought the car and had it towed home. At the time, I put a battery in and confirmed it was going to be a worthwhile project so it went right into the garage for a clutchectomy and lots of might as well jobs. Got the hazard switch wired up but fused brown wire to the switch was dead. Further investigation and the wire is toast up into the loom behind the dash. The PO had a cobbled up stereo installation in the console. Now I know why the radio didn’t work and the hazards as well. So it’s dash removal time.
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With the dash out now I could assess the state of affairs in the loom. Decided to tackle the burnt brown wire first so started removing the dried out blue tape at the console and on up to the brown wire cluster on the right side behind the pillow part of the dash. Dead wire had fused to some of the other wires but was able to separate individual wires to see that no other wires needed repair. A little electrical tape on a few where the insulation was thin just to play it safe.Clipped the soldered end where the brown wires were joined and replaced the burnt one. Soldered, heat shrink and a big wire nut for added measure. Wrapped new blue tape over all of the wire from console to the firewall end behind the wiper motor.
On to the crispy tach wires next. Peeled back the blue tape to sort out how far back and where the two individual wires ran. One to the coil across the dash and out through the firewall to passenger side. The other to a multiple bullet connection on the driver side. Fished a couple spare white wires out of my stash and soldered in a couple of repair sections, heat shrink, and re-wrapped the rest of the loom from the other repair area all the way to the driver side. Done.
This stuff was done a week or so ago and the thought was that I’d re-glue the cap back on and be done but it was such a gooey mess to try to clean up just to put a half-ass fix on so the thought process changed to sourcing a new pad and a few other goodies to put the dash pad to it’s former glory. Pillow dash detractors will argue it was never considered glorious but I rather like the fact it was only used for four production years. That in addition to it being a one year only split bumper car kind of makes it a little more unique. Next journal entry will detail the dash pad replacement learnings and installation.
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